
Anyway, during all that I decided to try taking the radiator out and flushing it through, but once I got it off noticed that it wasn't in the best of nick and was the old thinner version, so I swapped it out with a new 44mm one. Again, didn't make much noticeable difference. Also swapped out the thermostat for an 80C, this actually did seem to help a bit, but temps were only slightly lower and still too high for comfort, maybe about 3/4 on the gauge instead of 7/8ths. This was during warm weather right enough, on a more recent run when the air temp was at least 10C lower the gauge was closer to 2/3rds. Fan still runs almost constantly once warmed up (cleaned up the thermoswitch when I swapped the rad).
Doesn't seem to be losing any coolant, level stays pretty constant. Got hold of another CO tester and "sniffed" the header tank a couple of times, didn't detect anything it shouldn't.
Finally got around to checking the plugs after a decent run, having said that the van has only managed about 300 miles on these so not sure if that's enough to show anything useful yet. Not managed to check the timing with vac off yet due to bad weather, if I remember right it would stall when disconnecting or pinching the vac hose.


Thanks
David