Managed the next couple of miles to Go-Karting ok without excessive noise or smoke, just no power.
Upon leaving the Go-karting track I started up and still had no power, decided to swap the N75 valve for the N18 thinking it may be the actuator valve that had failed. When I tried to drive away I left a smokescreen which looked like something off of the 1980's batman programs.
After about 4 miles I had to give up as I was becoming a hazard to other road users.
Got carried the next 20 miles home on the back of a flatbed and only today managed to get a look at it. The following picture is the intake side of the turbo;

It should look like this...

Needless to say, the impeller has disintegrated and ingested parts of itself. There was probably 3-4mm of play in the rotor shaft, the exhaust turbine had fared any better and had clattered the VNT vanes so the whole thing was a write off, not even a new 'core' would save it.
The second turbo is my 'spare' but I'm going to fit something more suited to my engine, i.e. a VNT17 from a PD130.
Dave.