AAZ engine knock
Posted: 28 Jul 2016, 09:04
Hi
on a recent trip back from France the AAZ engine in my T25 developed an engine vibration/knock. Luckily we made it home and the problem didn't get any worse.
Last week I decided to remove the sump, and found what i thought was the problem, No 4 main bearing cap had snapped a bolt and was laying in the sump, so removed the bearing cap expecting much carnage but to my surprise no damage to the crank or bearing. Whilst getting ready to bolt the cap back up it broke in two, never seen that before.
I scourced another cap and some bolts from a freind, checked all the other caps and bolted it all back together, and have been putting some miles on it.
The problem is that under load there is still a vibration/ slight knock, not as bad but it is definitely there.
The crankshaft pulley end bolt is tight and was replaced when I did the conversion, it's running the JX exhaust manifold with new turbo, brickwerks oil cooler, lower temp t stat and has run faultlessly for the last four years.
My only thinking now is could it be the thrust bearings causing the crank to shuffle, ( I STUPIDLY DIDN'T CHECK THIS WHEN I HAD THE SUMP OFF).
Any ideas would be well received people.
Thanks
on a recent trip back from France the AAZ engine in my T25 developed an engine vibration/knock. Luckily we made it home and the problem didn't get any worse.
Last week I decided to remove the sump, and found what i thought was the problem, No 4 main bearing cap had snapped a bolt and was laying in the sump, so removed the bearing cap expecting much carnage but to my surprise no damage to the crank or bearing. Whilst getting ready to bolt the cap back up it broke in two, never seen that before.
I scourced another cap and some bolts from a freind, checked all the other caps and bolted it all back together, and have been putting some miles on it.
The problem is that under load there is still a vibration/ slight knock, not as bad but it is definitely there.
The crankshaft pulley end bolt is tight and was replaced when I did the conversion, it's running the JX exhaust manifold with new turbo, brickwerks oil cooler, lower temp t stat and has run faultlessly for the last four years.
My only thinking now is could it be the thrust bearings causing the crank to shuffle, ( I STUPIDLY DIDN'T CHECK THIS WHEN I HAD THE SUMP OFF).
Any ideas would be well received people.
Thanks