Not right after getting hot.
Posted: 22 Jun 2014, 19:27
Had a bad afternoon with Ritchie. 2.1 dj running carb and lpg. So...drove to northeast Friday....lovely run up van drove perfectly. ...whiny box....but that's all. Get to northeast and usual gas station shut. Very low on lpg So shoved some petrol in as had none on board. Got to lpg station ok and filled up. Drove back to parents. Next morning left to go to race track one-half hour away. Van seemed ok. Then drove to the doc shop. Van felt sluggish not wanting to accelerate through lower gears. Started to pop in exhaust when I depressed clutch to change gear. Get to 40mph and all seemed ok in 4 or 5 gear. Then I noticed that at 2500 revs (gear irrelevant) van would vibrate.....but nit just the steering...the whole dash was vibrating. Stopped completely at 2700 and was then fine. So got back to parents with the popping in exhaust at low revs low speed low gears. Not the usual backfire....more a ting sound. Let it cool checked leads and plugs...all tight....nothing lose. Water and oil ok.
So driving home today van with occasional pop and still a little sluggish but not as bad. Having done 50 miles decide to top up with lpg in case we had some bad lpg if that is even possible. Continue down the road. Then the issue start....suddenly can't get any more than 40mph in 5th going uphill...change down and it will pull again....then drove well for a while. ..then sluggish up a hill.
Now the fun started. Temp gauge started to rise....nothing serious but unusual so watch gauges like a hawk. Temp comes down. ...van drives fine. Coming off m11 to m25 temp shoots up...start to pull over...temp drops and stabilized at normal driving temp....decide to try and get to services. Then temp starts to climb...and heater went cold. Pulled over and stopped on hard shoulder as know that isn't good. Puddle by drivers wheel. Pooh. AA recovered to services and sorted connection with a couple of jubilee clips. Filled. Bled. Driven home with no further heating issues.
Will replace front to back pipes as the plastic end has broken so AA repair is not permanent.
But...the shuddering at 2500 revs still present as is the occasional sluggish feeling. Is this due to getting hot? Or the gear box starting to wear out. Also noticed fine oil marks on back door. ...hoping that the heat has thinned the oil and and oil change will stop this.
All the while we were filling and bleeding the engine wad running at 2200 to 2500 revs with no popping, no oil leaks. No nasty noises and was responsive to the throttle.
So....have I done it damage? The really weird thing is now it won't idle when the choke has come off. Could the heat have affected the log idle?
Thanks for reading....any more questions. Fire away!
Em xx
So driving home today van with occasional pop and still a little sluggish but not as bad. Having done 50 miles decide to top up with lpg in case we had some bad lpg if that is even possible. Continue down the road. Then the issue start....suddenly can't get any more than 40mph in 5th going uphill...change down and it will pull again....then drove well for a while. ..then sluggish up a hill.
Now the fun started. Temp gauge started to rise....nothing serious but unusual so watch gauges like a hawk. Temp comes down. ...van drives fine. Coming off m11 to m25 temp shoots up...start to pull over...temp drops and stabilized at normal driving temp....decide to try and get to services. Then temp starts to climb...and heater went cold. Pulled over and stopped on hard shoulder as know that isn't good. Puddle by drivers wheel. Pooh. AA recovered to services and sorted connection with a couple of jubilee clips. Filled. Bled. Driven home with no further heating issues.
Will replace front to back pipes as the plastic end has broken so AA repair is not permanent.
But...the shuddering at 2500 revs still present as is the occasional sluggish feeling. Is this due to getting hot? Or the gear box starting to wear out. Also noticed fine oil marks on back door. ...hoping that the heat has thinned the oil and and oil change will stop this.
All the while we were filling and bleeding the engine wad running at 2200 to 2500 revs with no popping, no oil leaks. No nasty noises and was responsive to the throttle.
So....have I done it damage? The really weird thing is now it won't idle when the choke has come off. Could the heat have affected the log idle?
Thanks for reading....any more questions. Fire away!
Em xx