Re: Non-T25: Buggy engine running problems
Posted: 21 Aug 2015, 09:20
PetenAli wrote:
As well as the coil the other key ignition part is the condenser. Only then can you say you've replaced all the ignitition side.
Sounds like you could do with a copy of the John Muir Bible. Apart from just being very useful its also a good read. Look here: http://www.amazon.co.uk/Keep-Volkswagen" onclick="window.open(this.href);return false; ... 1566913101
PS Its a pretty looking buggy - thanks for posting the pics!
Condenser noted, thank you.
"How to Keep Your Volkswagen Alive: A Manual of Step-by-step Procedures for the Compleat Idiot" - None taken! Thanks for the pointer - it does seem to get good write-ups.
The photos in this thread aren't my mate's, but I agree, they all look good. I'll get my mate's permission to post some photos. I'm particularly hoping to post a little video of the engine running - when we give it some beans it's fabulous. But at the moment there's an awful lot of popping from the right hand exhaust when we do that.
weimarbus wrote:As per your previous post where you said it was running well, if the only thing that you have done is to remove the manifolds to install new tin ware I would suspect that the tinware needs trimming back around the manifold seat to allow it to fit and bed down correctly, or is the fan shroud touching the carb and tilting it preventing a seal?
Yes, we did worry about that, since the manifold hole in the tinware is a tight fit, and the lip on the rocker side (as opposed to the spark plug side) is quite obstructive. So last night we eased the tinware up out of the way while fitting the manifolds. We pushed the manifold through the hole in the tinware, and tightened the nuts down completely, then repositioned the tinware. We even eased the lip on the manifold side out a little, using a pair of pliers, to make it easier to get the tinware back in place.
I'm pretty confident that we made a solid job of fitting those gaskets, so if there's an air leak, it's not at that point. If it wasn't for that blasted tinware we could spray it with WD40 while running to look for a leak, just to be sure, but I don't think that will work now.
The carbs have about a half inch gap to the shroud, and the carb-to-manifold gaskets are new. It's a bit awkward removing the left hand carb, since the 'inside' bolt has very tight access - we have to iterate with a ring spanner, then an open ender, then the ring again, then the open ender flipped over, just to turn it one flat! But the more I think about it, the more I'm inclined to swap the carbs over - that will narrow down the problem quite quickly.
What's annoying and puzzling is that we did indeed get it running properly after changing the gasket, but in all the work to refit the dynamo and the tinware the problem came back. It certainly did feel like we'd undone the good work of the new gasket. But I'm wondering now if we're looking at a coincidence. If there's, say, an electrical fault, perhaps disturbing all the plug leads, removing the dizzy cap etc, fixed it and brought it back in sync with the new manifold gaskets.